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I couldn't think or speak. I had a week
and a half to insure that this puppy ran. I could
sense fangs growing under my upper lip. I
began to snarl as my fingernail extended
beyond my cold hard hands. My eyes
reddened, and I wanted to ride. Without the
throttle cables I could use the cruise control, if
it still worked. I could jam it into gear and fly.
Frank hit me with a torque wrench. "We're
burnin' daylight," he snapped, "Let's measure
the cables and install the left Knuckle style
grip."
After wiping the grip end of the bar
down with alcohol, the grip interior was coated
with the rubber cement, that came with the
grips. Then it was immediately slipped into
place.
I snapped out of my Werewolf London
fog. We measured the clutch cable then
compared our findings with the throttle cables.
As I suspected, lucky 13 inches to make up for
the 12-inch taller bars that were an inch wider
than the stock units. Frank made a B-line for
the phone to call Barnett's and ordered the
cables. We were scheduled to roll up to the
fleet center for a performance upgrade on
Friday. It was Tuesday and the cables wouldn't
arrive until Thursday. It was going to be a
close call. "Barnett has been around since
Moby Dick was a minnow," Frank said. I've
been ordering custom cables from them since
I was in my 20s and first influenced by
Apehanger madness. "They are as reliable as
the sun on the coast," Frank continued, but I
was still nervous.
We weren't done yet. We torqued (15
foot pounds) the bars into place and began to
cut and fit Goodridge brakes hoses,
distributed by Barnetts and Custom Chrome.
Another delicate operation.
The King has dual disc brakes and the
fittings had to be installed just right, tightened
properly and finally torgued into place. From
the bottom of the triple-trees we used the
stock measurement to the calipers from the
existing junction under the trees. The new
lengths of Goodridge hose were cut with the
largest, strongest side cutters I had. Before
any fittings were installed we slipped a 2-inch
piece of black 3/8-inch diameter shrink tubing
over the hose. Next a chromed pinch fitting
was slipped over the cable. Frank brought the
tools and supplies including a tool to spread
the braided hose after the rubber housing was
stripped away to allow the new fitting to be
installed.
Stripping the rubber sleave back from
the end about an inch.
Here's all the components involved in
the process.
The tool used to spread the braided
steel shield.
Then a small brass round furl (like a
brass ball-bearing with a hole in it) is slipped
over the plastic lining. It must be pushed to the
point where the internal brass ridge meets
with the end of the plastic liner. The other half
of the fitting with the long tube is shoved into
place. In each case we clamped the fitting
between two sheets of leather then began to
tighten the sleeve onto the fitting. In each case
they were a bear to tighten down indicating
that we had succeeded in a strong, secure
grip.
The spreading process involves
shoving the tool into place and swiveling it to
make sure the braided area is spread
consistently.
Installing the furl is simple, just slip it
on carefully then push it into place. But,
inspect the inside to make sure the plastic
hose is against the interior ridge.
Now tighten the pinch fitting. Note the
leather pads in the vice to prevent damage to
the banjo fitting. These puppies are tough to
tighten down, take your time.
Here's another way to hold the banjo
fitting for final tightening. Be careful not to
bend or damage the sealing surfaces.
Note the two bronze washer/gaskets
on either side of the banjo fittings for proper
sealing which is critical to your brakes.
After each line was carefully constructed,
they were installed on the bike after some
jockeying with the Goodridge billet junction
under the tree which fit precisely.
For some reason, this Goodridge
junction mounted extremely snug between the
fork tube guards. For awhile we thought we
were in trouble.
We followed the original routing of the
stock brake line through the nacelle. With the
lines in place we torqued them down (17-20
foot pounds). I took the easy way of bleeding
the brakes. I pulled on the lever gently
allowing the bubbles to pass through the
master cylinder. It took a while, and I had to
keep filling the reservoir as the the lines
drained the supply.
We used the stock 12-point fittings
which torqued down easily to 17-20 foot
pounds, which seemed like a lot.
We had completed all that was possible
for Tuesday and I swung my leg over the
saddle once more. As fire and smoke poured
from my ears Frank crept out of the garage
and into the night.
Thursday morning I paced the vast
porch in front of the headquarters waiting for
the UPS man. The truck sped past without a
hint of slowing. I called Frank, he called
Barnetts. I called the Fleet center after finding
that the cables wouldn't arrive until Monday
morning, guaranteed. We had an American
Rider magazine deadline, but more
importantly I had a run-to-Arizona-deadline for
the following Friday. I started pacing the
garage and bowing to the new 16-inch apes. I
knew, by the power of the Ape, we would
succeed.
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