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Each part is powder coated twice and
sometimes three times. There is a base,
translucent for metallic, candy's, and clear for
depth and protection.
During the long day, while parts were
away, we took turns taking fasteners off the
diagram paper, sticking them in a sheet of
cardboard and spray painting the heads with a
heavy industrial gloss black.
We ordered the new fender mounted
license plate bracket, but when it arrived it had
a long strip of reflective tape along the bottom.
That 1/2-inch of metal had to be removed with
a hacksaw, filed flat then wet and dry sanded.
Then we sanded the chrome finish with 600
wet and dry and painted it with heavy gloss
black.
Drilling holes in the fender for the new
license plate bracket.
We needed to reshape the fender
bracket. It was designed to be installed
against the curve
of the fender above the taillight, but we moved
it below the taillight.
We used a two-part metal painting
process for best adhesion.
Ah, that bastard brake pedal. We finally
pried it loose, cleaned it with solvent, sanded
it and painted the sucker ourselves.
The mag wheels were mounted with Avon
Venom tires with a 150 strapped to the rear
rim. The Tires were balanced and we installed
the new floating rotors with black centers. My
plan was to add a taste of color to the wheels
with pinstriping. We discovered that the 150
was a tight fit for the King. It seems that later
model Softails and Dynas are set up for 150s
with narrower belts, not Touring models. We
had to space the pulley away from the wheel
.150 inch. Even then is was close. A bikernet
reader suggested that we machine the brake
caliper bracket .250-inch and add that amount
to the left side wheel spacer. Pablo from
Charolette H-D said that the rear wheels are
slightly off center, but the manual calls for the
front and rear wheel to be in line. I'm
investigating further. We also discovered a
problem with pinstriping the wheels. The new
H-D cast mag wheels are aluminum. My
striper, George, told us that the striping won't
last. Another source said that if I stripe then
clear it will hold. Still investigating.
Here's one of the spacers we used
which is about .050. It wasn't enough. Not
even close.
Here's a shot of one of the new rear
axle adjusters that pull the larger axle back
simultaneously. It's not easy though. I had to
set the bike on the ground as I tightened the
right side, but I had to hold the left side in
place or the belt adjustment changed.
An American Rider deadline was looming
ahead when the UPS man knocked on the
door and announced the arrival of the massive
powder coating box. I was relieved to have all
the parts back. I removed the spoked rear
wheel by snapping off the axle clip ring with a
small flat bladed screwdriver and loosening
the axle nut. We spun it to release the
pressure on the belt (from the left side). The
trick to removing the rear wheel was the brake
caliper. It seemed to lodge itself between the
rim and the swingarm. It took some fidgeting
to free the two elements. The new mag wheel
slipped into place easily. We discovered,
while returning the axle into position, that we
needed to insure the belt adjuster would
swing passed the shock mount, or it was
stuck.
We went at the installation like two kids
assembling a Christmas toy. We assembled
the turnsignals with a touch of industrial lube
to allow the plastic reflectors to slip back into
their rubber housings and into the black
shells. We referred to the factory manual for
torque specifications. Then I used Frank
Kaisler's wire tool (see tech tips in Wrench's
Garage) to hold the two wires in place so that I
could solder the junctions. "Don't forget to
slide on 1-inch of shrink tubing before you
solder these puppies," I told Nuttboy who was
fighting the other turnsignal into place with a
tiny Allen wrench.
Nuttboy ground and shaped the license
plate to fit the new bracket. The rear end was
looking trick as we plugged the connections
back together and replace the taillight. Then
using copious amounts of blue Loctite we
started to replace the bag roll bars, but didn't
tighten anything. We used our schematic on
the bench to insure we were grabbing the
correct fasteners and followed the parts from
the roll bars to the fender rails. (Note: that
during this process if you feel the need to
remove the rear axle in the near future, don't
tighten the lower bag rail. It interferes with the
axle.)
Once everything was in place, we
tightened the fasteners. About the time we
were leaning toward the Torx screws with a
ratchet Sin Wu sauntered into the garage and
pointed out a long strip of U-shaped rubber.
She has a knack for timing that uncanny. The
rubber strips back the saddlebag support
bracket. I also noted that the long piece goes
on the rear edge and the short piece on the
front. Once all the elements were in place and
aligned we started at the front and tightened
toward the back. The saddlebag quick-release
mounting brackets were also installed loose.
Then we placed the leather covered bags on
the bag rail and pushed the studs into place.
Only then could we tightened the mounting
bracket, 1/4-20, bolts. Watch that they don't
move during the last swing of the wrench.
Keep them in line with the bags or installing
and removing the bags will be a chore.
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